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dc.creator | DeBat, R. | |
dc.date.accessioned | 2010-06-16T16:25:16Z | |
dc.date.available | 2010-06-16T16:25:16Z | |
dc.date.issued | 2001-05 | |
dc.identifier.other | ESL-IE-01-05-37 | |
dc.identifier.uri | https://hdl.handle.net/1969.1/90950 | |
dc.description.abstract | Armstrong Service Inc. (ASI) conducted an engineered evaluation at an Ammonium Nitrate Manufacturing facility during the Fall of 1999. This plant manufactures Nitric Acid and high and low density Ammonia Nitrate. The purpose of this evaluation is to identify energy losses and system improvements in the steam and condensate systems. Steam system improvements focus on lowering the cost of steam, wherever possible, with paybacks of 3 years or less. Overall, this ASI evaluation identifies six (6) steam savings proposals with an average simple payback of 2.9 years. This evaluation also identifies one system deficiency that will lead to unnecessary expenditures if allowed to continue, but would help to increase production if the suggested improvement was implemented. The following report details the individual findings and outlines the corrections needed. The savings generated from these improvements will more than pay for themselves in short order. | en |
dc.language.iso | en_US | |
dc.publisher | Energy Systems Laboratory (http://esl.tamu.edu) | |
dc.subject | Steam and Condensate Systems | en |
dc.subject | Energy Evaluation | en |
dc.title | Savings in Steam Systems (A Case Study) | en |
dc.type | Presentation | en |
This item appears in the following Collection(s)
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IETC - Industrial Energy Technology Conference
Industrial Energy Technology Conference