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dc.contributor.otherTurbomachinery Symposium (47th : 2018)
dc.creatorMialkowski, Piotr
dc.date.accessioned2019-03-12T19:49:18Z
dc.date.available2019-03-12T19:49:18Z
dc.date.issued2018
dc.identifier.urihttps://hdl.handle.net/1969.1/175067
dc.descriptionCase Studyen
dc.description.abstractThis 15 MW steam turbine/gearbox/4-pole generator train, following a recent overhaul, was showing unusual phenomenon of high level 0.9X vibration during shutdown, as well as power limits due to vibration level increase. The case describes a single day* field investigation program, that lead to identification of the root cause of the problem and pin pointed other problems with the quality of the overhaul. Vibration data are reviewed showing solution through application of standard** methodologyen
dc.format.mediumElectronicen
dc.format.mimetypeapplication/pdf
dc.language.isoen
dc.publisherTurbomachinery Laboratory, Texas A&M Engineering Experiment Station
dc.relation.ispartofProceedings of the 47th Turbomachinery Symposiumen
dc.subject.lcshTurbomachinesen
dc.titleSteam Turbine with 0.9X Vibrationsen
dc.type.genreconference publicationen
dc.type.materialTexten
dc.format.digitalOriginborn digitalen


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