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    • Yu, John; Wang, Carl Feng; Yuan, Mingfeng; Péton, Nicolas; Guan, Xiaodong; Ye, Mingxing (Turbomachinery Laboratory, Texas A&M Engineering Experiment Station, 2021)
      Accelerometers were used to measure vibration of the input shaftusing an on-line remote monitoring system Though the vibrationamplitudes were below the acceptable limit for over a year period,two bearing damages were thought ...
    • Yu, John J.; Wang, Carl Feng; Yuan, Mingfeng; Peton, Nicolas; Guan, Xiaodong (Turbomachinery Laboratory, Texas A&M Engineering Experiment Station, 2022)
      A sudden step change in vibration was observed on a 7400 rpm compressor with direct amplitude from 43 um pp to over 62 um pp (trip level) at NDE, thus tripping the unit Vibration reached over 120 um pp at 4000 rpm, compared ...
    • Yu, John; Zhou, Tony Wei; Lin, Haibo; Wang, Carl Feng; Peton, Nicolas (Turbomachinery Laboratory, Texas A&M Engineering Experiment Station, 2018)
      This presentation provides a case study how to correctly deal with increased vibration on a steam turbine that drives a compressor. After the machine had not operated for a week, vibration level increased 5 times during ...