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dc.creatorSchmidt, John M.
dc.date.accessioned2022-08-31T16:21:52Z
dc.date.available2022-08-31T16:21:52Z
dc.date.issued2021
dc.identifier.urihttps://hdl.handle.net/1969.1/196747
dc.descriptionCase Study
dc.description.abstractA bolted raised face Joint (with O-ring gasket) was failure prone. An axisymmetric FEA (finite element analysis) of the Joint verified why: the flanges were not stiff enough (not thick enough); too much flange rotation occurred. A gap opened that the O-ring could extrude into and fail. Going with thicker flanges was not an option, but continuing with FEA, various flange profile designs were analyzed narrowing in on a profile that kept the flanges together at the gasket location, minimizing the extrusion gap. This design was implemented into the new replacement discharge head and was successful: The joint is now leak-free.
dc.format.mediumElectronicen
dc.format.mediumElectronic
dc.format.mimetypeapplication/pdf
dc.format.mimetypeapplication/pdf
dc.language.isoeng
dc.language.isoen
dc.publisherTurbomachinery Laboratory, Texas A&M Engineering Experiment Station
dc.relation.ispartofProceedings of the 37th International Pump Users Symposium
dc.titleA New Bolted Joint Profile, Optimized with FEA, Fixes a Leaking Propane Pump
dc.type.genreconference publication
dc.type.materialtexten
dc.type.materialText
dc.format.digitalOriginborn digitalen
dc.format.digitalOriginborn digital
dc.publisher.digitalTexas A & M University. Libraries
dc.publisher.digitalTexas A & M University. Libraries


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