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dc.contributorAsia Turbomachinery & Pump Symposium (2nd : 2018)
dc.creatorde Guarda Matos, Danilo
dc.date.accessioned2018-10-12T15:24:59Z
dc.date.available2018-10-12T15:24:59Z
dc.date.issued2018
dc.identifier.urihttps://hdl.handle.net/1969.1/172475
dc.descriptionCase Studiesen
dc.description.abstractThis failure lead a root cause analysis and a series of investigations that was taken place in a similar design unit deployed at a different site. This paper will describe the bump test and modal analysis procedures and results that were carried out on the end of all coils of the stator winding in the sister unit of the failed 360MW generator which lead to conclusions that were crucial for the determination it´s failure root cause.en
dc.format.mediumElectronicen
dc.format.mimetypeapplication/pdf
dc.language.isoen
dc.publisherTurbomachinery Laboratory, Texas A&M Engineering Experiment Station
dc.relation.ispartofAsia Turbomachinery & Pump Symposium. 2018 Proceedings.en
dc.subject.lcshTurbomachinesen
dc.subject.lcshPumping machineryen
dc.titleCatastrophic Failure Diagnosis with Modal Analysis of Generator Endwindingsen
dc.type.genreconference publicationen
dc.type.materialTexten
dc.format.digitalOriginborn digitalen


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