dc.contributor | Asia Turbomachinery & Pump Symposium (2nd : 2018) | |
dc.creator | de Guarda Matos, Danilo | |
dc.date.accessioned | 2018-10-12T15:24:59Z | |
dc.date.available | 2018-10-12T15:24:59Z | |
dc.date.issued | 2018 | |
dc.identifier.uri | https://hdl.handle.net/1969.1/172475 | |
dc.description | Case Studies | en |
dc.description.abstract | This failure lead a root cause analysis and a series of investigations that was taken place in a similar design unit deployed at a different site. This paper will describe the bump test and modal analysis procedures and results that were carried out on the end of all coils of the stator winding in the sister unit of the failed 360MW generator which lead to conclusions that were crucial for the determination it´s failure root cause. | en |
dc.format.medium | Electronic | en |
dc.format.mimetype | application/pdf | |
dc.language.iso | en | |
dc.publisher | Turbomachinery Laboratory, Texas A&M Engineering Experiment Station | |
dc.relation.ispartof | Asia Turbomachinery & Pump Symposium. 2018 Proceedings. | en |
dc.subject.lcsh | Turbomachines | en |
dc.subject.lcsh | Pumping machinery | en |
dc.title | Catastrophic Failure Diagnosis with Modal Analysis of Generator Endwindings | en |
dc.type.genre | conference publication | en |
dc.type.material | Text | en |
dc.format.digitalOrigin | born digital | en |