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dc.contributorAsia Turbomachinery & Pump Symposium (1st : 2016)
dc.creatorReddy, Ranga
dc.creatorReddy, Ravi S.
dc.date.accessioned2017-05-04T12:49:20Z
dc.date.available2017-05-04T12:49:20Z
dc.date.issued2016
dc.identifier.urihttps://hdl.handle.net/1969.1/160300
dc.descriptionCase Studyen
dc.description.abstractCase Study 15: This case study is about a typical experience where a steam turbine, which was running at 100 RPM on barring (turning) after overhaul, stopped abruptly and the rotor was found to be seized. The case study is about this incident and the external factors influencing the turbine rotor seizure, from 100 RPM to zero RPM in less than 5 seconds, its root cause and the rectification activities.en
dc.format.mediumElectronicen
dc.format.mimetypeapplication/pdf
dc.languageen
dc.publisherTurbomachinery Laboratories, Texas A&M Engineering Experiment Station
dc.relation.ispartofAsia Turbomachinery & Pump Symposium. 2016 Proceedings.en
dc.subject.lcshTurbomachinesen
dc.subject.lcshPumping machineryen
dc.titleAbrupt Stoppage of Turbine Rotor, Running on Barring after Major Overhaulingen
dc.type.materialTexten
dc.identifier.doihttps://doi.org/10.21423/R1S40S


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